Basics of Textiles, Research/ Review Paper, Textile Articles

Loom Down Time Reduction

Published on 
Author: TEXTILE VALUE CHAIN

Vilas Gharat

M.D. (Gharat & Associates.)

President (Textile Association India -Mumbai)

It has been observed that day by day Loom technology is improving at rapid speed resulting into very high-speed machines. There are many units installing such highspeed machines & unable to get desire production due to high machine down time.

Please find below Loom downtime analysis which has been carried out in one of modern weaving unit. The highest downtime is due to BEAM GAITTIG & hence I would like to present my paper on simple method of reduction of down time known as SMED.


What is S.M.D.

      It is known as SINGLE MINUTE EXCHANGE OF DIES & its Japanese technology developed by Mr. Shigeo Shingo. It is one of the lean methods for drastic reduction in changing time in production process.

It provides a rapid & efficient way of converting current product to next product in shortest time. It is “REVOLUTIONIZES BASIC CONCEPT OF ‘SET-UP CHANGE’.

Before explaining how it can be used in Beam Gaiting activities to reduce downtime, I would like to give you very common example of above method.

Generally, we require 5 to 10 mins to change car flat tire but in car race such as Formula One we observe all four tires & other activities are carried out by group of experts in few seconds. It is same method they are adopting known as SMED.

•  From the above it is very clear that we cannot afford to waste the time in a race. The operations are fast, tools are in its place and also man power

•        Replacing the Flat Tyre of Car

•        Find Jack, Tommy bar, spanner, in short tools.

•        Place & locate Jack below the car and lift the jack.

•        Loosen the nuts.

•        Remove the wheel

•        Bring another wheel

•        Locate & insert new wheel

•        Tighten the nuts.

•        Remove the jack & collect the tools.

•        Place it back in the car

•        Final tightening of the nuts

•        ABILITY TO DISTINGUISH: -

            It is very important to master the distinction between Internal & External activities. Please find chart of Internal & External activities of tire changing activities.


If you observe above chart you will notice that 50% activities are external which can be carried out earlier & kept ready to complete in actual changing time. The same method can be adopted in case of Beam Gaiting as mentioned below.

SMED FOR BEAM GAITING

     Please find below case study taken in one of modern textile unit having rapier looms with 20 shafts. Initially beam gaiting actual operations recorded in Video -noting step by step timings. Then the chart is prepared as mentioned below.

ACTIVITIES RECORDED OF FILM -

no.

START

END

TOTAL

activity

1




LOOM STOP

2

 

 


TENSION RELEASE/PKG REMOVAL/COVER OPENING

3

 

 

 

BEAM CUT/CLOTH WINDING/ TEMPLE LIFTING

4

 

 

 

REED REMOVAL

5

 

 

 

EMPTYING BEAM

6

 

 

 

BEAM UNLOADED

7

 

 

 

HEALD FRAME SUPPORT REMOVAL

8

 

 

 

REMOVING LENO AND MOUNTING ON STAND

9

 

 

 

TAKING AWAY EMPTY BEAM

10

 

 

 

TAKING OUT DROP PIN BARS

11

 

 

 

HEALD FRAME REMOVAL

12

 

 

 

SUCTION CLEANING STARTS

13

 

 

 

TAKING AWAYHEALD FRAME/ DROP PIN BAR AND REED

14

 

 

 

BRINGING CURTAIN

15

 

 

 

AIR CLEANING

16

 

 

 

WIDTH SETTING

17

 

 

 

FIXING REED PIECES

18

 

 

 

TAKING OUT OPENER

19

 

 

 

MAINTENANCE

20

 

 

 

SETTING TAPE GUIDE

21

 

 

 

REMOVING CURTAIN

22

 

 

 

MEASURING REED LENGTH / GREASING

23

 

 

 

TEMPLE PLATE SETTING / RAPIER HOOK FIXING

24

 

 

 

STROKE SETTING

25

 

 

 

CHECKING ALIGNMENT

26

 

 

 

BRINGING BEAM TROLLEY


27

 

 

 

BEAM LOADING STARTS

28

 

 

 

RAPIER FIXING(RH)

29

 

 

 

DROP-PIN FIXING  / COVER FIXING(RH RAPIER STROKE), FIXING BOTTOM H/F SUPPORT

30

 

 

 

ENDS STRAIGHTENING / TRANSFER TROLLEY OUT FROM LOOM

31

 

 

 

FIXING OF BEAM BARREL SUPPORT ROLLERS

32

 

 

 

PARALLELISING OF ENDS

33

 

 

 

BEAM LOCKED

34

 

 

 

REED FIXING

35

 

 

 

THREADING OF BEAM GAITING CLOTH

36

 

 

 

TYING OF KNOTS

37

 

 

 

HEALD FRAME TOP SUPPORT FIXING

38

 

 

 

PULLING OF WARP SHEET

39

 

 

 

RELOCKING OF BEAM

40

 

 

 

TEMPLE SETTING / THUMB ENDS FIXING / FEEDER THREADING

41

 

 

 

COVER FIXING (RH OPENER)/ BOTTOM H/F SUPPORT / SUCTION PIPE FIXING

42

 

 

 

MAIN MOTOR START / DESIGN FEEDING(PLAIN)

43

 

 

 

ENDS DRAWING STARTED

44

 

 

 

LOOM STARTED (PICKS INSERTED)

45

 

 

 

LENO FIXING (SPOOL)

46

 

 

 

LENO DEVICE FIXING

47

 

 

 

LENO SETTING

48

 

 

 

ENDS DRAWING STARTED IN HEALD WIRE

49

 

 

 

SPOOL ENDS DRAWING / DESIGN FEEDING / WEFT APPLIED AS PER PATTERN

 50

 

 

 

THREADING OF FALSE SEVEDGE

 51

 

 

 

MISSING HEALD WIRE FIXING

 52

 

 

 

LOOM STARTED / DROP PIN SUPPORT FIXING

 53

 

 

 

DOUBLE END AND PATTERN CHECKING (HEALD FRAME LIFTED IN SEQUENCE )

 54

 

 

 

LOOM STARTED

 55

 

 

 

CLOTH TORN

 56

 

 

 

WRONG DRAWN ATTENDED

 57

 

 

 

SAMPLE WORKED (FOR STOP MARKS )

 58

 

 

 

CONTRAST COLOUR SAMPLE WORKED

 59

 

 

 

LOOM  RUNNING IN

 60

 

 

 

SAMPLE CHECKING 0N SCREEN

 61

 

 

 

LOOM STARTED FOR PRODUCTION

Then all above activities are separated as Internal & External with time taken to complete those activities. The recorded film is shown in slow motion to team of loom shed beam gaiters’, fitters & supervisors. We had very long session of brain storming for how to carry out external activities in advance & execute at time of change in minimum time same as Formula 1 race video.

Finally, we carried out changes as per following chart & carried out following steps.

•        STEPS-1-PRESENT STATUS

•        VIDEO SHOOTING

•        STEP 2-

•        INTERNAL & EXTERNAL SET UP TIME

•        1. INTERNAL SET-UP.

•        THOSE ACTIVITIES WHICH NEED STOPPING THE EQUIPMENT,

•        LIKE, REMOVAL AND MOUNTING OF

•           BEAM.      

2. EXTERNAL SET-UP.

•        THOSE ACTIVITIES WHICH CAN BE CARRIED OUT WITHOUT STOPPING THE EQUIPMENT i.e. LOOM.


After conducting many trails, we could get following result with one-month summary. The earlier time for beam gaiting of 594 mins gradually reduced step by stem …

Step 1    594 Mins.

Step 2   269 Mins.

Step 3   112 Mins.

Final   49 Mins.

Saving 545 Mins. (9 Machine Hrs for every beam gating.)

SUMMARY



BEFORE

AFTER





SR.NO

AVG.TIME

594

45

 

 

 

 

1

INTERNAL ACTIVITY

60

22

 

 

 

 

2

EXTERNAL ACTIVITY

7

45

 

 

 

 

3

PARALLEL

30

47

 

 

 

 

 

TIME

112

49

Hope you understood it clearly.  Please visit our website  www.gharatandassociates.com or send mail to  gharatandassociates@gmail.com  OR vilasgharat@gmail.com in case of any inquiry.

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